Scale setup

Pokud se s námi chcete podělit o nastavení jednotky, je zde to právé místo.
mkgy
Posts: 13
Joined: Tue 15. Sep 2015 14:43:48

After much testing, there is still problem.

1. Sometimes stop for a moment the even at full rudder. Rudder servo: Align DS650




2. While pirouette sometimes the heli self aileron direction overthrown. Governance must be strong opposition.




I don't know what setup.
Thank you in advance for your help.
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sp7.4ds
Current setup
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ZeXx86
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Are you sure that the Pirouette Optimization is correct?
I understand that is is very hard to check it on the ground.

For example when you change rudder servo or rudder mechanics, it can be result for the opposite settings.
Spirit System developer
mkgy
Posts: 13
Joined: Tue 15. Sep 2015 14:43:48

The Pirouette Optimization setup correct. Do not every pirouette occur.
ZeXx86
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Are you sure that CG is good?
This can cause this issue as well.
Spirit System developer
mkgy
Posts: 13
Joined: Tue 15. Sep 2015 14:43:48

Then tested the rudder servo ball farther.
mkgy
Posts: 13
Joined: Tue 15. Sep 2015 14:43:48

CG correct. Main rotor shaft vertical.
mkgy
Posts: 13
Joined: Tue 15. Sep 2015 14:43:48

The problem may not be that counterclockwise rotation of the rotor?
ZeXx86
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This shouldn't be a problem.

Does it happen always only to one side only?

Where is your collective pitch when you are hovering? (approx. position)
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mkgy
Posts: 13
Joined: Tue 15. Sep 2015 14:43:48

It occurs in both directions.
Hovering approx 4-5 degree.
ZeXx86
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It really looks like there is wrong pirouette optimization direction.
This behavior exactly correspond with the state when it is configured in opposite direction.

How did you tested that it is configured properly?
Maybe after initial configuration you have changed Sensor compensation direction for Rudder - this will lead in the problem that it is reversed.
Spirit System developer
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