Hello,
Yes I do firstly all that , Compass calibration , than I try the idea you told me with Compass Heading
correction, I start with minus values until 40% and the Heli in Position Hold still glitch, I change the value to plus 40% and the Heli stops now glitching and Hold the position, but lose altitude very fast even with stick full Throttle,
I was then start to adjust with vertical gain and when I was in the value 90% the Heli goes faster down,
I notice with 40% value the Heli goes slower down. Also it's strange with the Function Position Hold with Pitch active that the Heli lose altitude and not react to the stick input. The point is that I have this problems only on the GOBLIN 500, on the GOBLIN Big Kraken works fine since installation.
